The Greenpower Diary unfortunately
has not been updated for a while now and
I am sorry if you keep coming back to it
and nothing has changed! The plan is that
one of the students has designed a website
for the team and that information will be
available on there instead of the diary.
This can be found at www.thecragrat.co.uk.
Matt will put a students perspective of
our activities on his site but I thought
as a diary swansong that I would give you
a teachers view of events leading up to and
on the day of the national final.
Rockingham
The story starts before the Midlands heat
held at Rockingham Speedway in July. Steady
progress had been made on the car but a concerted
effort was needed to get the car ready to
race. As usual we had big plans for improvements
from the previous year! Unfortunately new
building work above the D & T Department
(and a fire!) stopped us getting on with
this as well as expected. We were fortunate
in having a speed controller made for us
by Harrison-Croft Electronic Solutions and
Dave from Marell had designed a module that
would display volts, amps, and motor temp
on an LCD screen which would also act as
the rear view mirror in conjunction with
a rear pointing camera. Everything was working
really well until Saturday morning when some
fine tuning of the system was to take place.
On switching on the car, the motor ran at
full speed instantly and the throttle did
not seem to work. It transpired that some
components on the controller had inexplicably
failed. Dave kindly agreed to have a go at
repairing this for us but hopes were not
high that it would be done for the Tuesday
race. This was the case so as a stop gap
we fitted the car with a simple on/off push
button working through a relay. The unfortunate
thing was the time it took messing about
with this was going to be used to sort out
the current display. This would be really
important to us as we needed this to know
how fast to go on our batteries and when
to change gear. This was not working!
Tuesday morning arrived and the car was
ready for its lift down to Rockingham with
SKS Racing. A massive thank you to Peter
for doing this for us!! The journey to Rockingham
was very straightforward with Mr. Keeble
and Mr. Hutchinson sharing the driving of
the school minibus, with Mr. Bolger a very
nervous passenger!
I am not going to go into massive details
about the race only to say that the car ran
smoothly and apart from a spin and a relay
failing (again) we had no major problems.
The batteries did not last the four hours
as we suspected they wouldn’t. Having
to guess the gear to run was not a perfect
situation. We also nearly got wiped out by
a school who cheated by taking a shortcut
on a part of the circuit which was not being
used and then coming suddenly back onto the
proper circuit directly in front of the Rat!
The car did just over 70 miles and we were
pleased with this as it was just a shakedown
run. I must say that the Rockingham Circuit
is superb and would make an ideal venue for
one of the major Greenpower events.
Needless to say our day was not over! On
the way back up North, with Mr. Keeble driving,
the bus lost all power. Fortunately it picked
up again and we carried on. Mr. Hutchinson
then drove and when in the outside lane of
the A1 overtaking a lorry, the power went
again only this time it did not come back
on! Fortunately we were able to make it onto
the hard shoulder. A two hour delay whilst
a very nice man came and fixed the bus.
Preparation for the final
The next day and some decisions to make!
Would the current car be a challenger? If
not what would we need to do? We knew we
would have until mid September to get everything
sorted. It was decided that we would build
a new bodyshell, change the wheels, and the
size of the chain and sprockets amongst other
things. We knew that we can use a couple
of weeks of the summer holidays to do this
and everything will be ready for the Croft
heat in mid September. How wrong we were!
The ongoing building work turned the department
into a no go area. Dust, mess, noise etc
etc!
We arrived back at the start of September
with a hard decision to make. Do we try and
get the car ready for the Croft race or hope
that we had made the final from our Midland
heat, and plan for this? A hard decision
was taken to miss Croft. We then had just
over a month to sort everything out and an
anxious wait until the last heat to see if
we had qualified for the final!
Progress on the car was steady and decisions
taken about roll bars, instrument mounts,
etc. The body was a real pain and although
it was made on the car and in one piece,
when it was cut it would not fit anymore!
Time was passing and although Saturday mornings
were used to continue, there were just not
enough hours in the day. With just a week
to go, Dave of Marell kindly agreed to come
into school to try and sort the speed controller
(which he had repaired and reprogrammed)
especially important was the current usage
which we hoped would appear on the screen.
This was finally sorted at about 9.15 just
as the school was plunged into darkness after
Open Evening. The bodyshell was sprayed up
the next evening by Mr. H and Lewis and the
decals applied on Thursday. With only a few
small things to finish on the Friday, hopes
were high that the car and gear could be
taken and stored in one of the school’s
outbuildings ready for collection on Sunday
morning. Unfortunately when switching on
the electronics for a final check, nothing
worked! Some anxious telephoning to Dave
did not sort the problem and he kindly agreed
to come in for another Saturday morning to
sort this out with Mr. H. (Mr. H passes him
tools and makes the tea!) Some stray wires
and blown fuses were the cause and were soon
sorted. The car was taken up to be stored
right on the 12 noon deadline for school
to close for the weekend. We then decided
that giving the car a run around the car
park would be a good idea just to make sure
everything was ready for the race. With no
students around, (ahem Tom and James!) Dave
sat on the side bars and proceeded to drive
around. This was brilliant and everything
was going fine until…. A shout, thump
and crash as Dave ran into a kerb with the
car! The speed controller had failed again.
Working only with the tools we were taking
to Goodwood as the school was closed, a relay
and on/off push button were added. The cooling
fan had also blown and a new one wired to
12v instead of the 24v of the original. This
work was finished at 2.00pm.
The National Final
The gang met at 4.30 am ready
for the long journey down to Goodwood Circuit
on the south coast. This time we would be
travelling in style thanks to Dr. Walton
who very generously allowed us to hire a
coach for the day. Graham the driver would
be doing all the hard work! Miss Thompson
and Miss Freeman took advantage of the space
and wrapped in duvets, heads on pillows,
jim jams on, and sleep masks in place, they
immediately went to sleep, and Miss Freeman
especially, would be on the Olympic sleeping
team if there was one! The journey was extremely
uneventful and after a couple of short stops
we arrived at the circuit at approximately
10.30. After transferring our gear and car
across the track on a trailer because the
bus would not fit through the tunnel, we
were ready for action……not!
Some work that we were unable to do on Saturday
(ahem again Tom and James!) needed to be
done at the circuit.
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This was mainly bleeding
the brake which only took a couple of minutes.
Mr Bolger and Matt also did a repair to
the broken bodywork caused when the speed
controller failed. With this done, we decided
we would adjust the safety belts and Sarah
our tallest driver was put in the car. She
did not fit! Because of the late finishing
of the car and using Tom with his short legs
for our measurements, Sarah although only
2” taller had longer legs and she would
just not fit in the car. Several things were
tried including putting the links above the
steering column but this only made the car
turn right when steering left! Eventually
by removing the seat back, side bars, ammeter
and adjusting the brake cable, we got Sarah
to fit. Right for scrutineering! Pulling
the car backwards out of the garage highlighted
another problem as the wheel rubbed against
the body. An inspection the next day showed
that the accident had bent the steering support
bar but this was not noticed at the time!
A longer screw was used in the steering stop
and this cured this. The unfortunate thing
was that all these modifications and repairs
were taking time and as we were doing this
the parade was called. A decision was made
to miss the parade and get the car scrutineered
ready to race. Again foiled again! The scrutineering
bay was empty as the scrutineers thinking
their day was over had gone to watch the
parade!
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Crag Rat was hurried onto the
track at the very back of the parade but
at least the guys got chance to show off
the car and the fabulous fleeces that Miss
Barrett had spent
her free time embroidering.
Finally tracking down the scrutineers, Crag
Rat was presented and after a nervous couple
of minutes was passed to race. Just as the
sticker was put on the car, the horn sounded
for the race to get underway. As the race
starts in waves and our grid was 17 rows
back we still had time to get there! Pushing
the car onto the track we found that someone
had moved into our grid spot and subsequently
we had been shuffled back to 71st position,
the last one on the grid! Once the car is
out on track, there is little that the watchers
can do but wait for news of progress (or
not!).
Expecting a steady climb through
the field, imagine our shock, when with Tom
driving, after the first lap, the car went
past in 10th place!! A massive improvement
of 61 places! Using our drivers in rotation
was the fairest way of meeting with the rules
and giving everyone a fair go. This seemed
to be unlike some of our main rivals who
did not seem to be stopping at all. I guess
that they will have their conscience to live
with as the less pitstops you do, the bigger
advantage you gain! We seemed to be competing
with ILMT tractor for the most improved car with
no one else in the running.
Anyway back to the action!
Crag Rat easily lasted the two hours on he
first set of batteries. Running in 10th and
9th places it was always on the fringe of
the top ten. I think that this is in some
part due to the excellent hospitality provided
by Miss Freeman and her superb trolley although
it took some desperate pleading by the circuit
announcer when it was not in the pit area
at the correct time. The battery change although
slow, started our second two hour stint.
With some extremely good driving in the first
two hours by Tom, David, Ryan (except for
the chicane!) and Josh, it was now Sarah’s
turn. With instructions to use a higher gear
for more speed, Sarah was going to do a 45
minute stint. Some excellent and consistent
laps saw us move into eighth place and consolidate
our position of most improved. ILMT had now
moved out of the top twenty and we knew that
we would only need to be seven places higher
than them to get the most improved. Sarah
swapped with David and again a good and consistent
45 minute run saw us move into 7th place.
Part of this was misfortune which befell
our competitors but with Crag Rat not missing
a beat, this was testament to the excellent
engineering and design on the car by the
guys, Mr Marriott and Mr Hutchinson. The
final 30 minutes saw Tom back in the car.
Listening to the commentary, we realised
that we were on the same lap as the car coming
fifth. With a little look we could easily
catch them. Alas! It was not to be and indeed
a couple of recovering cars went past us
in the last ten minutes as our batteries
started to fail.
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Our final position of ninth (or was it eighth?)
was our best result in a national final.
We also did over a hundred miles which earned
a silver award. The car was the best performing
from the North and has achieved the highest
mileage from a Northern car under the new
F24 regulations. We are also delighted to
say that we won the trophy for most improved
gaining 46 places from our start number.
The coach was loaded in record
time and a smooth ride home saw the happy
but tired team arrive back in Knaresborough
at 12.15. By the time parents had collected
students, most of the teachers had been up
for 22 hours (except for Miss Freeman who
slept all the way home) Was it worth it?
You betcha!
Loads of people are involved in KJS’s
Greenpower Challenge attempt and I would
like to thank them all for their help!
Our Sponsors
- Dave at Marell without whom……
- Gordon and Pat at Claro Precision Engineering
- Elliot Harrison-Croft from Harrison-Croft
Electronic Solutions for the speed controller.
- Dalton Joinery
- Knaresborough Lions
- Knaresborough Rotary Club
KJS
- Robert Marriott
- Alan Bolger
- Rachel Thompson
- Sami Freeman
- Dr Walton
- The Maintenance staff
- The Bursars
Pit Crew and Young Engineers
Drivers
- Tom
- Sarah
- David
- Ryan
- Josh
Future plans? Watch this space!
Mr Hutchinson